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Gulf of Mexico Region

Pipeline Incidents – 2004 (8 Total)

January 14, 2004 – Shell Deepwater Development Inc.

MMS Investigation Report:

 None

Activity:

Development / Production

Lease:

G15879

Event(s):

Pollution (13 bbls hydraulic Fluid, Methanal and corrosion inhibitor)

Area:

 Garden Banks

Operation:

Production/ Workover / Pipeline Segment No. 14170

Block:

 341

Cause:

Human Error

Rig/Platform:

 Noble Jim Thompson

Water Depth:

2011

Remarks: The eighth of nine anchors for the semi-submersible drilling rig, Noble Jim Thompson came in contact with Shell’s subsea Habanero No. 1 well umbilical (segment no. 14170) as the anchor was being positioned. One hydraulic flying head and two electric flying heads sustained damage. 10 bbls of HD 540 hydraulic fluid, 3 bbls of methanol, and 10 gals of corrosion inhibitor were released. The No. 1 well was shut-in at the time of the rig move and no well liquid/gas hydrocarbons were released. The No. 1 well is 64,952 feet from the GB 426, Auger host platform.


January 29, 2004 – Seneca Resources Company 

MMS Investigation Report:

 None

Activity:

Development/

Production

Lease:

 G22271

Event(s):

 Pollution (7 bbls condensate)

Area:

 High Island

Operation:

 Pipeline Segment No. 14301

Block:

A 345

Cause:

External Damage /Leak

Rig/Platform:

 N/A

Water Depth:

232

Remarks: The pipeline was slightly damaged by an anchor drag. A dive vessel was retrieving anchors prior to moving off location in 5 foot seas. During anchor recovery operations, the pipeline was snagged and a gas/condensate release occurred. The volume in the pipeline was estimated to be 23 bbls, 7 bbls of which were lost. The spill came from the tree that was damaged by the anchor drag.

16-Feb-2004 Williams Field Services Gulf Coast Co.
(Also Listed as a Fire)

MMS Investigation Report:

None

Activity:

Development/
Production

Lease:

G03472

Event(s):

Fire

Area:

Brazos

Operation:

Production

Block:

A20

Cause:

Human Error

Rig/Platform:

A

Water Depth:

129 feet

Remarks: Williams Pipeline was in the process of relocating a pipeline from the jacket structure to the seafloor, so the jacket could be salvaged. During the operation hot work was being conducted. Apparently welding slag/sparks ignited tarp material and was quickly extinguished by the fire watch. Williams Pipeline reported that there were no injuries or property damage (other than the tarp material).


09-Mar-2004 – Shell Deepwater Production, Inc.        

MMS Investigation Report:

None

Activity:

Development/Production

Lease:

G07493

Event(s):

Fatality (1)

Area:

Garden Banks

Operation:

Laying flowlines

Block:

427

Cause:

See USCG report

Rig/Platform:

None

Water Depth:

2860 feet

Remarks: Preliminary reports indicate that a roustabout on a derrick barge sustained fatal injuries when he was struck by a section of pipe that fell as it was being moved from the pipe bin to the pipe preparation rack. The section of pipe fell uncontrolled to the pipe preparation rack due to a failure of the after hook on the crane hoist hook lifting device.  The USCG is investigating this incident.


May 22, 2004 – Equilon Pipeline Company LLC 

MMS Investigation Report:

 Pending

Activity:

Development/

Production 

Lease:

 G07963

Event(s):

Flex Joint Failure/Pollution (4 gal. oil)

Area:

 Mississippi Canyon

Operation:

 Pipeline Segment 10360

Block:

807

Cause:

Equipment Failue

Rig/Platform:

 A – Mars

Water Depth:

2933 feet

Remarks: A four gallon spill was associated with a flex joint failure.


June 5, 2004 – Anadarko E&P Company LP 

MMS Investigation Report:

None

Activity:

Development/

Production 

Lease:

G02109

Event(s):

Pollution (39.64 bbls oil)

Area:

Eugene Island

Operation:

Pipeline Segment No. 1188

Block:

306

Cause:

Leak

Rig/Platform:

A

Water Depth:

 200 feet

Remarks: A Pinhole leak was found in the submerged portion of the pipeline.


August 4, 2004 – Anadarko E&P Company LP

MMS Investigation Report:

 None

Activity:

Development/

Production 

Lease:

 G12941

Event(s):

 Pollution  (10 bbls oil)

Area:

 Ship Shoal

Operation:

 Pipeline Segment No. 13453

Block:

 129

Cause:

 Leak

Rig/Platform:

 N/A

Water Depth:

  45 feet

Remarks: A Pinhole leak was found in the submerged portion of the pipeline.


November 10, 2004 – W & T Offshore, Inc.
(Also Listed as a Collision)

MMS Investigation Report:

None

Activity:

Production

Lease:

G13938

Event(s):

Collision

Area:

South Timbalier

Operation:

Production

Block:

229

Cause:

Human Error

Rig/Platform:

A

Water Depth:

200  feet

Remarks:  A 165 foot crew boat collided with the A Platform. Navigational aids lights were flashing at the time of the collision and the platform lights were illuminated. The platform had minor damage.  The platform had 6 slots for wells and one subsea well that was tied back to the structure. The incoming pipeline and umbilical cord of the subsea well were slightly damaged but were not leaking.

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Last Updated: 10/19/09, 11:52 AM