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Incidents 1996-2005
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 Content:
    Melinda Mayes

 Pagemasters:
    OMM Web Team

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  Gulf of Mexico Region

Fires – 1997

January 03, 1997 - Exxon Corporation

Investigation: None Activity: Exploration
Lease: G03091 Event(s): Fire
Area: Matagorda Island Operation: Drilling
Block: 632 Cause: Equipment Failure
Rig/Platform: Ensco 90 Water Depth: 69’

Remarks: An electrical panel shorted out when a plug on the saltwater relief valve rusted. The salt water sprayed into a 480-volt panel causing electrical sparking in the panel. The relief valve for this saltwater system, the electrical panel, and the circuit breakers have all been replaced. Estimated cost: $500.00


January 04, 1997 - CXY Energy, Inc.

Investigation: Complete Activity: Development
Lease: 00138 Event(s): Fire
Area: West Delta Operation: Production
Block: 45 Cause: Equipment Failure/Human Error
Rig/Platform: G Water Depth: 49'

Remarks: Compressor lost o-ring seal. Fire started. Damaged compressor building. Fire out at approximately 2045 on January 5, 1997. Started rest of platform. Both compressor areas isolated.


January 14, 1997 - Conoco, Inc.

Investigation: None Activity: Development
Lease: 00175 Event(s): Fire
Area: Grand Isle Operation: Production
Block: 43 Cause: Equipment Failure
Rig/Platform: AA Compressor #3 Water Depth: 110’

Remarks: Sparks ignited small flame (2-3 in). Used 30-lb dry chemical extinguisher. All hot work is suspended.


January 16, 1997 - MOBIL Expl&Prod SE, Inc.

Investigation: Complete Activity: Development
Lease: G01366 Event(s): Fire
Area: Main Pass Operation: Production
Block: 92 Cause: Human Error
Rig/Platform: A Water Depth: 24'

Remarks: The operator observed a fire at the top of the uniflux surge tank and the uniflux exhaust stack. The operator woke the two contractors to help fight the fire. They activated the fire pump and directed a fire monitor towards the top of the uniflux surge tank PSV and uniflux exhaust stack. The fire was extinguished and the uniflux pumps and blowers were manually shut down.


January 16, 1997 - MOBIL Expl&Prod SE, Inc.

Investigation: Complete Activity: Development
Lease: G01366 Event(s): Fire
Area: Main Pass Operation: Production
Block: 92 Cause: Human Error
Rig/Platform: A Water Depth: 24'

Remarks: The operator observed a fire at the top of the uniflux surge tank and the uniflux exhaust stack. The operator woke the two contractors to help fight the fire. They activated the fire pump and directed a fire monitor towards the top of the uniflux surge tank PSV and uniflux exhaust stack. The fire was extinguished and the uniflux pumps and blowers were manually shut down.


January 21, 1997 - Pennzoil Exploration & Production Company

Investigation: Complete Activity: Development
Lease: G02439 Event(s): Fire
Area: East Cameron Operation: Production
Block: 335 Cause: Equipment Failure
Rig/Platform: A Water Depth: 280'

Remarks: Damaged rental air compressor shut in and will be sent in to beach for a replacement unit.


January 28, 1997- Chevron USA, Inc.

Investigation: Complete Activity: Development
Lease: G01196 Event(s): Fire
Area: South Marsh Island Operation: Production
Block: 61 Cause: Equipment Failure
Rig/Platform: A Water Depth: 118'

Remarks: Rented portable light plant at junction box had electrical fire. Noticed fire within minutes and extinguished it.


January 31, 1997- Chevron USA, Inc.

Investigation: Complete Activity: Development
Lease: G01147 Event(s): Fire
Area: Vermillion Operation: Production
Block: 246 Cause: Equipment Failure
Rig/Platform: D Water Depth: 128'

Remarks: The fire was caused by a broken nipple on the compressor suction scrubber, which caused gas to blow from the compressor and deflect off the heliport and then become ignited by the exhaust system of the compressor.


February 02, 1997 - Texaco Exploration & Production, Inc.

Investigation: None Activity: Development
Lease: G06358 Event(s): Fire
Area: Garden Banks Operation: Production
Block: 189 Cause: Equipment Failure
Rig/Platform: A Water Depth: 720'

Remarks: Small fire in the area of the compressor starter. The fire lasted approximately 2-3 minutes before it was extinguished using a 30-lb handheld unit. Normal production operations were being conducted at the time the compressor shut-in on a fire loop. Follow-up on February 3rd, vibration caused wear on sparkplug wire. Gas regulator was leaking, providing fuel source. Texaco replaced 4 plug wires and replaced the gas regulator. After testing and receiving verbal permission platform was put back on line.


February 05, 1997 - Shell Offshore, Inc.

Investigation: None Activity: Exploration
Lease: G12981 Event(s): Fire
Area: South Timbalier Operation: Drilling
Block: 296 Cause: Equipment Failure
Rig/Platform: POOL 18 Water Depth: 282’

Remarks: Short in generator function box. Generator burned up. Used CO2 extinguisher to put out fire.


February 06, 1997 - Conoco, Inc.

Investigation: Complete Activity: Development
Lease: 00175 Event(s): Fire
Area: Grand Isle Operation: Other
Block: 43 Cause: Equipment Failure/Human Error
Rig/Platform: AA – Compressor #3 Water Depth: 100'

Remarks: Welding on ac main deck. Welding sparks ignited instrument gas leaking from fisher gas regulator. Used 30-lb dry chemical fire extinguisher. Regulator's diaphragm developed a leak allowing gas to be released from upper bonnet spring case vent hole. Lasted a few seconds. Fusible plug melted on instrument gas line and produced second fire.


February 12, 1997 - Unocal Exploration Corporation

Investigation: None Activity: Development
Lease: G02646 Event(s): Fire
Area: East Breaks Operation: Production
Block: 159 Cause: Equipment Failure
Rig/Platform: A Water Depth: 924’

Remarks: Small fire was discovered on the glycol reboiler. Smoke came from insulation and shut off the fuel gas to the burner. The fire was quickly put out with water and no pollution or injury occurred. Fill at glycol developed cracks and leaked out on insulation causing the fire. Nipple has been replaced and the unit was placed back on production.


February 14, 1997 - Shell Offshore Inc.

Investigation: None Activity: Development
Lease: G02015 Event(s): Fire
Area: West Cameron Operation: Production
Block: 565 Cause: Human Error
Rig/Platform: A Water Depth: 200’

Remarks: Smoke and flames were noticed behind the chemical skid. A 30-lb fire extinguisher was used to put out the flames. There was no pollution released or injury to personnel. The cause of the circuit overload, which they suspect caused the flame, is being investigated.


February 16, 1997 - Shell Offshore Incorporated

Investigation: Complete Activity: Exploration
Lease: G13614 Event(s): Fire
Area: South Marsh Island Operation:

Drilling

Block: 204 Cause: Equipment Failure
Rig/Platform: Diamond Ocean Concord Water Depth: 441'

Remarks: Transformer shorted out, which caused the coating to melt and drop on some blue prints that ignited. The fire was put out with no further damage.


February 18, 1997 - Enron Oil & Gas Company

Investigation: None Activity: Development
Lease: G03079 Event(s): Fire
Area: Matagorda Island Operation: Production
Block: 555 Cause: Equipment Failure
Rig/Platform: A Water Depth: 75’

Remarks: The fire was started by a short in an old shielded electrical cable that ignited hydraulic oil drippings from one of the crane hoses. The fire was immediately extinguished using a hand-held dry chemical unit. No injuries or damages were reported. New stainless steel braided shield-type was installed as cable of choice for use in high movement areas.


February 18, 1997 - OXY USA, Inc.

Investigation: Complete Activity: Development
Lease: G02665 Event(s): Fire
Area: Brazos Operation: Production
Block: A-133 Cause: Equipment Failure
Rig/Platform: A Water Depth: 204'<

Remarks: A "dresser coupling" on the oil connecting line to the externally mounted "Oberg" oil filter parted, allowing engine oil to spray onto the exhaust manifold and ignite. The operators were able to extinguish the fire utilizing two 30-lb hand-held fire extinguishers and one 350-lb ansul unit. Total damage is estimated at $500 with no injuries or loss of production. To insure that incidents of this nature be eliminated, all external oil filters are being inspected on OXY operated platforms, and any "dresser couplings" will be replaced with either hard piping or armored flex pipe.


February 18, 1997 - Phillips Petroleum Company

Investigation: None Activity: Development
Lease: G02712 Event(s): Fire
Area: High Island Operation: Production
Block: A-561 Cause: Equipment Failure
Rig/Platform: A Water Depth: 255’

Remarks: Glycol reboiler was shut down after a drip was noticed. The reboiler was monitored, and 6 hrs later a small amount of smoke was observed in the PSV connection. The flame was extinguished with a freshwater hose. There was no pollution or injury that occurred. The operator will clean and repair as necessary.


February 19, 1997 - Shell Offshore Incorporated

Investigation: Complete Activity: Development
Lease: G04424 Event(s): Fire
Area: Vermillion Operation: Production
Block: 221 Cause: Equipment Failure
Rig/Platform: A Water Depth: 111'

Remarks: Platform shut-in on a process upset. Operator was in the process of bringing the platform on production when the fire occurred. Process problem was corrected, compressor was restarted and in the process of being loaded with gas when a noise (backfire) was heard and fire was seen at the stack above the turbine compressor/engine. Engine stopped or was shut down by the safety system, and the fire was extinguished.


February 28, 1997 - Marathon Oil Company

Investigation: Complete Activity: Development
Lease: G02572 Event(s): Fire
Area: Vermillion Operation: Production
Block: 331 Cause: Equipment Failure/Weather
Rig/Platform: 1 Water Depth: 260'

Remarks: The generator oil heat exchanger system was shut down for repairs but the generator was left running. After isolating the oil system from the heat source, the butterfly valves were locked out of service, and the block valves were closed. The oil was subsequently drained from the segment to be repaired. Leaking valves and flanges were unbolted but not taken out of line. The generator was shut down by the smoke detector when the fire alarm announced a fire in the generator room. The fire was extinguished with water and chemical.


March 03, 1997 - Callow Petroleum Operating Company

Investigation: Complete Activity: Development
Lease: G06842 Event(s): Fire
Area: Chandelier Area Operation: Production
Block: 40 Cause: Equipment Failure
Rig/Platform: A Water Depth: 108'

Remarks: The operator noticed a small flame 2 ft-3 ft high on the side of the glycol reboiler surge tank on the second deck of the platform. He got a 30-lb dry chemical extinguisher and told his assistant to shut in the reboiler. The fire was extinguished but reignited due to the heat from the surge tank. Water was applied to the tank to soak the insulation and cool the tank. The heat from the reboiler surge tank was the only possible ignition source determined.


March 04, 1997 - Elf Exploration, Inc.

Investigation: Complete Activity: Development
Lease: G01670 Event(s): Fire
Area: Main Pass Operation: Production
Block: 293 Cause: Human Error
Rig/Platform: A Water Depth: 247'

Remarks: Small fire on glycol dehydration system. Safety system (fusible plug in the loop) shut platform in. Little slug of condensate was dumped out of glycol line into still column of reboiler, which vented out of top and ignited on the exhaust stack on the reboiler. Slight damage to glycol control panel.


March 07, 1997 - Union Oil Company of California

Investigation: Complete Activity: Development
Lease: G01034 Event(s): Fire
Area: Ship Shoal Operation: Production
Block: 266 Cause: Equipment Failure
Rig/Platform: A Water Depth: 179'

Remarks: The operator noticed a small fire on the engine exhaust muffler of oil shipping pump No. 2. It was extinguished with a 30-lb handheld fire extinguisher. The fire was a result of the threads on the pump's PSV test kit cracking due to excessive vibration of the pump.


March 13, 1997 - Union Oil Company of California

Investigation: Complete Activity: Development
Lease: G01034 Event(s): Fire
Area: Ship Shoal Operation: Production
Block: 266 Cause: Equipment Failure
Rig/Platform: A Water Depth: 179'

Remarks: A fire occurred when the threads on a PSV on an oil pump cracked. Oil sprayed on the engine exhaust. The fire was quickly extinguished with chemicals, water, and foam. Minor damage was caused by the fire. Paint and control tubing was the extent of the damage.


March 13, 1997 - Phillips Petroleum Company

Investigation: Complete Activity: Development
Lease: G01198 Event(s): Fire
Area: South Marsh Island Operation: Pipeline
Block: 66 Cause: Equipment Failure
Rig/Platform: A Water Depth: 129'

Remarks: Construction activity was being conducted approximately 10 ft above and 10 ft horizontally from the area that the fire occurred. Slag from hot cutting work fell onto a pipeline expansion tank flange resulting in ignition of leaking natural gas. A 3-in flame was noticed by the fire watch and extinguished with one hand-held extinguisher. All hot work ceased and further work was done by cold-cut method. The area and flanges were sniffed prior to commencement of hot work/construction activities.


March 15, 1997 - Pennzoil Exploration & Production Company

Investigation: None Activity: Development
Lease: G12803 Event(s): Fire
Area: West Cameron Operation: Production/Completion
Block: 580 Cause: Equipment Failure
Rig/Platform: Main Pass I Water Depth: 243’

Remarks: During testing of newly completed well, rapid blowdown of test separator into a 100-bbl stock tank caused gas to vent through a 4-in vent line. The vent line was pointing down to within 8 in of the skid pan. The venting gas was possibly ignited by static electricity or trash in the vent line or skid pan. The fire was put out within 5 minutes by rig personnel, and no injuries occurred.


March 22, 1997 - Chevron USA, Inc.

Investigation: Complete Activity: Development
Lease: G02047 Event(s): Fire
Area: East Cameron Operation: Workover
Block: 272 Cause: Equipment Failure
Rig/Platform: A Water Depth: 185'

Remarks: A rental air compressor was being used to power air pumps that fill volume tanks with sea water as a working fluid for coiled tubing operations. The air compressor had been in operation for approximately 1 hr. While closing off air pressure to the air pumps it was noticed that the electrical wiring to the air compressor high temperature shut down switch had ignited and was burning the wire insulation. The air compressor was shut down, and the fire was extinguished by holding a rag over the temperature switch. The flame flared up from the wire insulation, approximately ½ in above the temperature switch and burned only momentarily.


March 24, 1997 - Marathon Oil Company

Investigation: Complete Activity: Development
Lease: G02061 Event(s): Fire
Area: East Cameron Operation: Production
Block: 321 Cause: Equipment Failure
Rig/Platform: A Water Depth: 220'

Remarks: A fire occurred as a result of overheated coastal Thermalane 600, which is used as a heat transfer medium in the waste heat recovery unit. Thermalane, which had leaked into the waste heat recovery unit drip pan, became stagnant due to a clogged drain line and apparently autoignited. A post fire pressure test of the unit identified leaks on a seal located on the hot oil pump and a valve bonnet flange. Both leaks were contained in the drip pan. The fire self- extinguished, and the damage was very minor.


March 31, 1997 - Mobil Oil Exploration & Production SE, Inc.

Investigation: Complete Activity: Development
Lease: G02947 Event(s): Fire
Area: Main Pass Operation: Production
Block: 73 Cause: Equipment Failure
Rig/Platform: A Water Depth: 174'

Remarks: While servicing the glycol system, a workman noticed there was no glycol returning from the contact tower. The contactor gave a high-level indication, and it was noted that the glycol reboiler was overfilled. An overflow was experienced, and the glycol system was shut-in. During the investigation of the glycol problem, a weak point was found around the base of the glycol refill nipple. The glycol refill nipple was repaired, the glycol return problem was solved, and the system was put back into service. Later that night, the insulation around the glycol reboiler ignited and began to burn.


April 01, 1997 - American Exploration Company

Investigation: Pending Activity: Development
Lease: G10638 Event(s): Fire/Loss of Well Control
Area: East Cameron Operation: Production/Drilling
Block: 328 Cause: Equipment Failure/Human Error
Rig/Platform: Pride 1001 E Water Depth: 243'

Remarks: Prior to the loss of well control, the rig crew had set and cemented casing and the BOP stack was being nippled down with four bolts remaining when annular flow was observed. All personnel were safely evacuated onto the standby workboat. The rig and platform were on fire and the derrick collapsed. Clean up marine vessels were notified when there appeared to be an apparent oil spill.


April 01, 1997 -  Enron Oil & Gas Company

Investigation: None Activity: Development
Lease: G03466 Event(s): Fire
Area: Matagorda Island Operation: Production
Block: 713 Cause: Human Error
Rig/Platform: A Water Depth: 109’

Remarks: Flash fire in generator room when welder was installing rebuilt generator. Fire was immediately extinguished. No injuries or damages.


April 07, 1997 - Conoco, Inc.

Investigation: Complete Activity: Development
Lease: 00182 Event(s): Fire
Area: West Delta Operation: Production
Block: 70 Cause: Human Error
Rig/Platform: A Water Depth: 120'

Remarks: A roof, supported by scaffolding, was formed with 2 in x 6 in boards spaced about 12 in apart and covered with a canvas tarpaulin. The inside edge of the tarp was secured to the scaffolding at a height of about 3 ft from the deck and pulled over the roof supports. The excess was rolled up and tied along the outer edge of the roof with a portion resting on the well-insulated turbine exhaust. The wind loosened the ties causing the tarp to extend over the end of the turbine exhaust. The tarp ignited and flames traveled down the length of the structure. Burning material was ingested into the turbine causing it to shut down.


April 09, 1997 - Vastar Resources, Inc.

Investigation: Complete Activity: Development
Lease: G01608 Event(s): Fire
Area: South Pass Operation: Production
Block: 60 Cause: Equipment Failure
Rig/Platform: A Water Depth: 190'

Remarks: The 3-stage turbine gas compressor was taking an unusual amount of time to load up and start working at its normal capacity. While the operator was trying to bring the compressor into full service, the auxiliary seal oil pump was in recycle, which put unusual stress on the bearings in the pump. The bearings in the pump failed causing a metal-to-metal seal, which resulted in friction in the pump. There was also an o-ring seal failure, which allowed oil to escape from the pump while the metal-to-metal friction resulted in a small fire. The mechanic immediately shut down the compressor and extinguished the fire with a 30-lb dry chemical extinguisher.


April 11, 1997 - Stone Energy Corporation

Investigation: Complete Activity: Development
Lease: 00775 Event(s): Fire / Explosion
Area: Vermillion Operation: Drilling
Block: 131 Cause: Human Error
Rig/Platform: Sundowner Dolphin 110 Water Depth: 60'

Remarks: None


April 14, 1997 - Unocal Exploration Corporation

Investigation: Complete Activity: Development
Lease: G04000 Event(s): Fire
Area: South Timablier Operation: Production
Block: 53 Cause: Human Error
Rig/Platform: A Water Depth: 62'

Remarks: The fill valve on the fill line to the lubricating oil day tank for Generator #1 was left open. The tank for this generator was part of an oil fill manifold in which the lube oil pump was located on the top deck of the platform, and the generator tank was located on the lower deck. The oil fill pump on the top deck began pumping oil into the oil fill manifold to fill the day tank for the compressor on the same deck, while oil migrated down to the lower deck and began filling the day tank for Generator #1. The tank on the lower deck overfilled and spilled oil onto the exhaust pipe of Generator #1. A fire started setting off fire alarms and shutting in the platform. The fire was extinguished using a 30-lb dry chemical fire extinguisher and water for cooling.


April 16,  1997 - Allwaste Oilfield Services, Inc

Investigation: None Activity: Development
Lease: G01633 Event(s): Fire
Area: Main Pass Operation: Production
Block: 133 Cause: Human Error
Rig/Platform: A Water Depth: 180’

Remarks: Trianthelene glycol ignited. Insulation damaged. Used water hose to put out fire. Lasted approximately 5 minutes.


April 16, 1997 - Unocal Exploration Corporation

Investigation: Complete Activity: Development
Lease: 00297 Event(s): Fire
Area: Vermillion Operation: Production
Block: 26 Cause: Human Error
Rig/Platform: A Water Depth: 30'

Remarks: While cutting out a pan to remove a tripping hazard, a piece of hot slag flew through the grating. The area was sniffed for gas, and there was a fire watch upstairs and downstairs. The phi fueling system, located just below the pan, was covered with wet tarps and being sprayed with fire hoses. The pump supply was still hooked up with polly flow. A small leak in the polly flow allowed an accumulation of natural gas to build up under the protective tarp, which ignited when a piece of cutting slag fell on the tarp. The fire hose was used to put the flash fire out within seconds.


May 01, 1997 - Marathon Oil Company

Investigation: None Activity: Development
Lease: G01449 Event(s): Fire
Area: West Delta Operation: Production
Block: 79 Cause: Equipment Failure
Rig/Platform: A Water Depth: 112’

Remarks: Gaslift compressor turbo charger had developed a leak, and oil leaked from the turbo onto insulation. Insulation caught fire due to excessive heat. No damage to equipment. Turbo charger on order. Employee nearby saw smoke and immediately shut down compressor and extinguished fire using 30-lb dry chemical and water to cool.


May 14, 1997 - Vastar Resources, Inc.

Investigation: None Activity: Development
Lease: G02137 Event(s): Fire
Area: South Pass Operation: Workover
Block: 60 Cause: Equipment Failure
Rig/Platform: A Water Depth: 185’

Remarks: None


May 15, 1997 - Vastar Resources, Inc.

Investigation: None Activity: Development
Lease: G02137 Event(s): Fire
Area: South Pass Operation: Workover
Block: 60 Cause: Equipment Failure
Rig/Platform: A