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 Content:
    Tommy Perry

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    OMM Web Team

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  Gulf of Mexico Region

Fires – 2004 (66 incidents total)

01-Jan-2004 Chevron/Texaco

MMS Investigation Report:

None

Activity:

Development/
Production

Lease:

G05911

Event(s):

Fire

Area:

Green Canyon

Operation:

Crane-Production

Block:

205

Cause:

Human Error

Rig/Platform:

A

Water Depth:

2590 feet

Remarks: After performing routine maintenance on the crane, antifreeze was spilled on the crane exhaust which caught fire. The fire was small and was extinguished with one bucket of water. There were no damages or injuries.


6-Jan-2004 Eni Petroleum Exploration Company

MMS Investigation Report:

None

Activity:

Development/
Production

Lease:

G01088

Event(s):

Fire

Area:

West Delta

Operation:

Production

Block:

89

Cause:

Equipment Failure

Rig/Platform:

 A

Water Depth:

220 feet

Remarks: A small flash fire occurred at the platform. The No. 2 turbine generator exhaust located inside the generator room came into contact with a lubricating oil when leaked onto the turbine exhaust, which resulted into a small flash fire. There were no injuries to personnel or damage to the platform.


7-Jan-2004 Devon SFS Operating, Inc.

MMS Investigation Report:

None

Activity:

Development/
Production

Lease:

G07825

Event(s):

Fire

Area:

Main Pass

Operation:

Production

Block:

255

Cause:

Equipment Failure

Rig/Platform:

 A

Water Depth:

332 feet

Remarks: Mechanic states that he lost power in the building which is supplied by Hanover Generator, not the Platform Generator. He then proceeded outside to see what was wrong and found that the No. 2 generator had sparks and flames coming out of the generator end. He then pushed the fire alarm button, shut in the compressor, and grabbed a fire extinguisher to put out the fire.


12-Jan-2004 BP American Production Company

MMS Investigation Report:

None

Activity:

Development/
Production

Lease:

G0133

Event(s):

Fire

Area:

Grand Isle

Operation:

Production

Block:

47

Cause:

Human Error

Rig/Platform:

C

Water Depth:

88 feet

Remarks: With the platform shut in, a construction crew was torch cutting deck plate on the top deck to replace it with grating. A gas lift header on the deck below, in the vicinity of the fuel gas skid had been isolated and bled down. A flame resistant tarp was placed over the gas lift header, which was also surrounded on 3 sides with 8' high plywood walls. A fire watch was stationed in the area and spraying water on the tarp while the hot work commenced. Sparks/slag was falling on the tarp. The fire watch and another worker noticed a fire under the tarp and proceeded to extinguish it with a fire extinguisher and a water hose. There were no injuries, no harm to the environment and only minor damage to a Barton chart recorder as a result of the fire.


21-Jan-2004 Denbury Offshore Inc.

 

MMS Investigation Report:

None

Activity:

Development/
Production

Lease:

G02027

Event(s):

Fire

Area:

West Cameron

Operation:

Production

Block:

639

Cause:

Equipment Failure

Rig/Platform:

A

Water Depth:

362 feet

Remarks: A construction crew was cutting out rusted nuts and bolts on the firewater pump muffler flanges. Some hot molten slag fell on the inlet starting gas line to the starter. A small fire was put out with a 30 lb. extinguisher. After investigating, it was found that a nipple in the inlet starting gas line was leaking.


21-Jan-2004 Denbury Offshore Inc.

MMS Investigation Report:

None

Activity:

Development/
Production

Lease:

G02027

Event(s):

Fire

Area:

West Cameron

Operation:

Production

Block:

639

Cause:

Equipment Failure

Rig/Platform:

A

Water Depth:

362 feet

Remarks: A Denbury employee was observing construction work and noticed smoke in the rental compressor engine compartment. The starter was still engaged and the wiring was on fire. The employee put out the fire with a 30 lb. extinguisher.


29-Jan-2004 Denbury Offshore Inc.

MMS Investigation Report:

None

Activity:

Development/
Production

Lease:

G04268

Event(s):

Fire

Area:

West Cameron

Operation:

Production

Block:

648

Cause:

Equipment Failure

Rig/Platform:

A

Water Depth:

375

Remarks: While performing hot work on a vessel, a small fire was started due to some oil floating on top of water used to flood the pan under the vessel. The fire was extinguished by the fire watch using a 30 lb. dry chemical extinguisher.


30-Jan-2004 Anadarko Petroleum Corp.

MMS Investigation Report:

None

Activity:

Development/
Production

Lease:

G18402

Event(s):

Fire

Area:

Green Canyon

Operation:

Production

Block:

608

Cause:

Human Error

Rig/Platform:

A

Water Depth:

4320 feet

Remarks: A small fire occurred when a tarp that was covering the aluminum insulation barrier on the Heat Media Expansion tank was ignited by slag from a cutting torch. Personnel were cutting scaffolding brackets around the crane. Fire was extinguished by fire watch within 30 sec. The only damage was to the tarp. Alarm sounded and everyone reported to proper areas. The area sprayed with firewater hose to make sure all areas were covered.


16-Feb-2004 Williams Field Services Gulf Coast Co.

MMS Investigation Report:

None

Activity:

Development/
Production

Lease:

G03472

Event(s):

Fire

Area:

Brazos

Operation:

Production

Block:

20

Cause:

Human Error

Rig/Platform:

A

Water Depth:

129 feet

Remarks: Williams Pipeline was in the process of relocating a pipeline from the jacket structure to the seafloor, so the jacket can be salvaged. During the operation hot work was being conducted. Apparently welding slag/sparks ignited tarp material and was quickly extinguished by the fire watch. Williams Pipeline reported that there were no injuries or property damage (other than the tarp material).


17-Feb-2004 El Paso Production Oil & Gas Company

 

MMS Investigation Report:

None

Activity:

Development/
Production

Lease:

G02412

Event(s):

Fire

Area:

High Island

Operation:

Production

Block:

317

Cause:

Human Error

Rig/Platform:

A

Water Depth:

217 Feet

Remarks: Workers were in the process of repairing a leak between the temporary quarters and the permanent quarters, which are attached. While trying to repair the leak, hot welding slag fell and started a fire in the lower permanent quarters. The fire alarm sounded, and a fire extinguisher and water hose were used to extinguish the fire. Two rooms of the permanent quarters were damaged. There were thirteen people on board. There were no injuries or pollution.


19-Feb-2004 Chevron Texaco Corp.

MMS Investigation Report:

Completed

Activity:

Development/
Production

Lease:

G02388

Event(s):

Fire

Area:

High Island

Operation:

Production

Block:

 A 563

Cause:

Equipment Failure-External Damage

Rig/Platform:

B

Water Depth:

305 feet

Remarks: A small fire occurred at the south end of the Glycol Reboiler on the "B" platform. There were no injuries or pollution (all fluids were contained). There was minor equipment damage, estimated at less than $1000 (the tin strip holding the insulation was damaged on the Glycol Reboiler). The leak was due to a pin hole leak from a weld on the reboiler.


22-Feb-2004 BP Exploration Inc.

MMS Investigation Report:

Completed

Activity:

Development/
Production

Lease:

G05800

Event(s):

Fire

Area:

Ewing Banks

Operation:

Production

Block:

826

Cause:

Human Error

Rig/Platform:

A

Water Depth:

495 feet

Remarks: An operator was performing casing pressure diagnostics on a well. He was bleeding off pressure from the well through a ½-inch needle valve into a plastic DOT drum using stainless steel tubing. Apparently static electricity ignited the condensate being bled in to the plastic drum. During the process, the operator noticed flames coming from drum and tried to close the needle valve. He was unable to close valve. The fire was extinguished with a 30 lb fire extinguisher and fire water hose. The needle valve was then closed.


23-Feb-2004 Denbury Offshore Inc.

MMS Investigation Report:

None

Activity:

Development/
Production

Lease:

G02027

Event(s):

Fire

Area:

West Cameron

Operation:

Production

Block:

639

Cause:

Human Error

Rig/Platform:

A

Water Depth:

362 feet

Remarks: Field personnel reported a small fire resulting from welding and burning operations. The incident involved cutting operations where hoses from cutting rig came in contact with hot slag. The fire watch used a 30 lb. extinguisher to put the fire out on the hoses.


25-Feb-2004 Forrest Oil Corp.

MMS Investigation Report:

None

Activity:

Development/
Production

Lease:

G03393

Event(s):

Fire

Area:

Vermillion

Operation:

Completion

Block:

102

Cause:

Human Error

Rig/Platform:

Diamond Ocean Spur

Water Depth:

70 feet

Remarks: Quality Preheat was attempting to heat a wellhead to 3500 F. The wellhead was sitting on a wooden pallet and it began to rain, so a tarp was placed over the wellhead to prevent it from cooling. The tarp was left on after the rain subsided. The welder walked around the corner to the trash compactor then noticed smoke and flames coming from around the wellhead. The fire was extinguished with three CO2 fire extinguishers. There were no injuries and the only damages were to the tarp and pallet.


26-Feb-2004 BP Exploration Inc.

MMS Investigation Report:

None

Activity:

Exploration

Lease:

G09982

Event(s):

Fire

Area:

Green Canyon

Operation:

Drilling

Block:

826

Cause:

Equipment Failure

Rig/Platform:

Diamond Ocean Confidence

Water Depth:

6560 feet

Remarks: A 1/4 inch bleed plug on a fuel injection pump in the No. 8 engine blew out, spraying fuel on the overhead exhaust manifold. A flash fire occurred when the fuel contacted the manifold. The engine's own fire detection and suppression system came on and extinguished the fire. A fire team was mustered when the fire alarm sounded. The fire team monitored the area to allow the engine to cool and all emergency phone calls were made. A small amount of spilled fuel was cleaned from the area and no pollution entered the Gulf. There were no fatalities, injuries or equipment damage.


09-March-2004 Chevron Texaco Corp.

MMS Investigation Report:

None

Activity:

Development/
Production

Lease:

G02047

Event(s):

Fire

Area:

East Cameron

Operation:

Production

Block:

272

Cause:

Equipment Failure

Rig/Platform:

D

Water Depth:

182 feet

Remarks: Superior Energy Services wire line personnel was in the process of pulling gas lift valves out of the well, when the wire line helper noticed a burnt smell and then saw a small flame coming from the wire line unit starter solenoid. The fire was extinguished with a 30 lb fire extinguisher. The starter was sent to Guidry's Ignition Service where the starter was taken apart. The evaluation of the starter revealed corrosion inside the solenoid, which caused the starter’s bendix gear to stay engaged to the fly-wheel and generate a high voltage and enough heat to cause the fire.


13-March-2004 Chevron U.S.A. Inc.

MMS Investigation Report:

None

Activity:

Development/
Production

Lease:

G00819

Event(s):

Fire

Area:

Ship Shoal

Operation:

Production

Block:

168

Cause:

Human Error

Rig/Platform:

B

Water Depth:

50 feet

Remarks: Upon installation of a wind generator, an electrical short to the ground occurred, discharging the energy of the batteries and igniting the insulation on the battery jumpers. The cause was found to be a positive termination in the wind generator conduit junction box  that was installed without insulation. The lack of a circuit breaker between the batteries and the fault location allowed the current to continue for duration sufficient to ignite the battery jumper insulation. Recommended actions to prevent this in the future: Only electrically skilled personnel shall terminate wiring circuits. Each termination shall be inspected to ensure termination meets NEC. All I&E crews shall be provided with detailed installation drawings prior to beginning installation.


13-March-2004 Amerada Hess Corp.

MMS Investigation Report:

None

Activity:

Development/
Production

Lease:

G01449

Event(s):

Fire

Area: