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 Content:
    Melinda Mayes

 Pagemasters:
    OMM Web Team

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  Gulf of Mexico Region

Fires – 2002 (total 87)

02-Jan-2002 - Shell Offshore Inc.

MMS Investigation Report:

None

Activity:

Development/Production

Lease:

G05868

Event(s):

Fire

Area:

Mississippi Canyon

Operation:

Production

Block:

809

Cause:

Equipment Failure

Rig/Platform:

/ A (URSA TLP)

Water Depth:

3,800 feet

Remarks: Employee smelled something burning in process module as he walked through the area. He noticed sparks from motor on the pump for heat media fluid. It is suspected that the bearing overheated and caused sparking. Plastic cooling fan caught fire. Pump was shut down and fire was extinguished with a hand-held chemical fire extinguisher. Damage was minimal.


 05-Jan-2002 - Exxon Mobil Corporation

MMS Investigation Report:

None

Activity:

Development/Production

Lease:

G01083

Event(s):

Fire

Area:

West Delta

Operation:

Production

Block:

73

Cause:

Human Error

Rig/Platform:

/A

Water Depth:

87 feet

Remarks: A small fire occurred as a door latch was being repaired on top of the production water polishing floatation cell. A drill was being used to drill a hole in the door when it generated a spark that ignited the atmospheric gas in the floatation cell vessel. The fire was extinguished within one minute with a fire water hose. There were minimal damages.


05-Jan-2002 - BP Amoco Corporation

MMS Investigation Report:

None

Activity:

Exploration

Lease:

G14658

Event(s):

Fire

Area:

Mississippi Canyon

Operation:

Drilling

Block:

822

Cause:

Human

Rig/Platform:

Ocean Confidence

Water Depth:

6,255 feet

Remarks: Welders were cutting a pad eye on a beam in the No. 6 caterpillar room on the rig when the heat ignited a personnel basket stored in the engine room. The fire was detected and extinguished immediately with minor damage.


12-Jan-2002 - Shell Offshore Inc.

MMS Investigation Report:

None

Activity:

Exploration

Lease:

G12166

Event(s):

Fire

Area:

Mississippi Canyon

Operation:

Drilling

Block:

765

Cause:

Human Error

Rig/Platform:

M & P 204/

Water Depth:

3,800 feet

Remarks: A contract employee observed a small flame on the top deck of the facility and reported it to the deck coordinator. Upon investigation, it was determined that a scaffold board was on fire. The fire was extinguished within five minutes with a water hose. The board had been placed too close to an engine exhaust during some construction work.


15-Jan-2002 - Transcontinental Gas Pipe Line Corporation

MMS Investigation Report:

None

Activity:

Development/Production

Lease:

00560

Event(s):

Fire

Area:

Vermilion

Operation:

Pipeline Segment No. 1576

Block:

67

Cause:

Other – Pipeline rupture

Rig/Platform:

/ B

Water Depth:

40 feet

Remarks: The operator reported a pipeline rupture with a fire on the water.  Within 2 hours Transco confirmed it was their gas pipeline and had it shut in.  No injuries or pollution.


16-Jan-2002 - Devon Energy Corporation

MMS Investigation Report:

None

Activity:

Development/Production

Lease:

G02416

Event(s):

Fire

Area:

High Island

Operation:

Production

Block:

A 325

Cause:

Equipment Failure

Rig/Platform:

/A

Water Depth:

229 feet

Remarks: Production hand noticed a small fire on the glycol reboiler. Fire was put out and situation under control in 35 minutes. Seven 20 lb. and one 150 lb. units were used to put out the fire and keep the fire from flashing until the glycol unit cooled sufficiently. After unit was cooled, the insulation was pulled back to reveal a nipple with two holes ¼ inch in diameter. Glycol had been spraying on hot surface which caused the fire.


21-Jan-2002 - BP Amoco Corporation

MMS Investigation Report:

None

Activity:

Development/Production

Lease:

G03596

Event(s):

Fire

Area:

Grand Isle

Operation:

Production / Other – welding

Block:

20

Cause:

Equipment Failure / Human Error

Rig/Platform:

B/

Water Depth:

77 feet

 

Remarks: A construction crew was conducting a hot work operation when a piece of hot slag fell onto a windbreak tarp, and the tarp catching it on fire. It was extinguished immediately by the fire watch and a rigger with two 30 lb. dry chemical fire extinguishers.


22-Jan-2002 - Chevron U.S.A. Inc.

MMS Investigation Report:

None

Activity:

Development/Production

Lease:

G01260

Event(s):

Fire

Area:

South Timbalier

Operation:

Production

Block:

177

Cause:

Equipment Failure

Rig/Platform:

E /

Water Depth:

105 feet

Remarks: Slag from an overhead cutting torch ignited a small flow of escaping gas from a wellhead cap. The flame was about 3 inches high and was extinguished with a 1 gallon jug of water by the welder.


23-Jan-2002 - Pogo Producing Company

MMS Investigation Report:

None

Activity:

Development/Production

Lease:

G16493

Event(s):

Fire

Area:

Main Pass

Operation:

Production

Block:

61

Cause:

Equipment Failure

Rig/Platform:

A /

Water Depth:

135 feet

Remarks: The engine coolant for a gas compressor leaked onto the compressor engine turbo charger (1100 degrees). This created a small flash fire that extinguished itself immediately.


29-Jan-2002 - Chevron U.S.A. Inc.

(also listed as Injury)

MMS Investigation Report:

Completed

Activity:

Development/Production

Lease:

00373

Event(s):

Fire / Injury (1)

Area:

Main Pass

Operation:

Production

Block:

40

Cause:

Equipment Failure / Human Error

Rig/Platform:

/ P

Water Depth:

48 feet

Remarks: Worker went to the Master Control Panel to investigate why the system (natural gas) pressure was low. He opened up the back of the panel to troubleshoot the loss of pressure, in an attempt to locate the gas leak and correct the problem. The worker checked the panel vent ports and found no leakage. At about this time, he felt heat (hot flash) to his face and arms. He immediately shut the panel doors to contain the heat. Apparently the fire was brief and self extinguished immediately due to lack of fuel. The worker was then evacuated by helicopter for medical care. The employee was treated for first and second degree burns.


31-Jan-2002 - Agip Petroleum Exploration Co. Inc.

MMS Investigation Report:

None

Activity:

Development/Production

Lease:

G07049

Event(s):

Fire

Area:

Green Canyon

Operation:

Production

Block:

254

Cause:

Equipment Failure

Rig/Platform:

/ A (Allegheny Sea)

Water Depth:

3,315 feet

Remarks: While conducting a ground fault test on the generator, a fire occurred. The CO2 deluge system was used to extinguish the fire. The cause of the fire is unknown at this time.


02-Feb-2002 - BP Exploration Inc.

MMS Investigation Report:

Completed

Activity:

Development/Production

Lease:

G02919

Event(s):

Fire

Area:

Ship Shoal

Operation:

Production

Block:

91

Cause:

Equipment Failure

Rig/Platform:

/A

Water Depth:

30 feet

Remarks: Contract personnel on the main deck observed a fire at the water bath heater area. The maintenance personnel shut in the compressor and a platform ESD occurred at about the same time. They used 30 lb. bottles to extinguish the fire within a few seconds.


04-Feb-2002 - BP Amoco Corporation

MMS Investigation Report:

Completed

Activity:

Development/Production

Lease:

G02919

Event(s):

Fire

Area:

Ship Shoal

Operation:

Production

Block:

91

Cause:

Human Error

Rig/Platform:

/ A

Water Depth:

13 feet

Remarks: Operator went to fill day tank. He opened a series of valves, which overfilled the crank case and went into manifold and subsequently went into exhaust. A small flame around the insulated muffler located on top of the generator enclosure. The platform operator initiated an ESD on the platform and initial emergency response was also initiated. The fire was extinguished utilizing hand held dry chemical units and the platform’s potable water system.


07-Feb-2002 - Chevron U.S.A. Inc.

MMS Investigation Report:

None

Activity:

Development/Production

Lease:

G15563

Event(s):

Fire

Area:

Green Canyon

Operation:

Production

Block:

237

Cause:

Equipment Failure

Rig/Platform:

/ A (Typhoon Seast)

Water Depth:

2,150 feet

Remarks: The primary generator shut down due to a platform ESD involving the platform glycol system. After troubleshooting the ESD, it was necessary to start the emergency generator to bring the facility back online. When the emergency generator was brought back on line, operators noticed smoke coming from the emergency generator enclosure. There was a small fire as a result of a backfire in the emergency generator engine. This backfire caused the exhaust filter element to catch fire. The generator was shut down and the fire was extinguished using a portable CO2 unit.


07-Feb-2002 - Exxon Mobil Corporation

MMS Investigation Report:

None

Activity:

Exploration

Lease:

G08211

Event(s):

Fire

Area:

East Breaks

Operation:

Completion

Block:

945

Cause:

Equipment Failure

Rig/Platform:

Glomar Celtic Sea/

Water Depth:

4,628 feet

Remarks: Personnel heard a loud noise, and then the winch starting unspooling wire. The brakes were in the applied position. The heat generated form the brake band ignited line tar off of wire causing a small fire. After the wire finished unspoooling, the fire was immediately extinguished. No personnel were injured and no apparent damage to equipment occurred.


12-Feb-2002 - Vastar Resources, Inc.

(also listed as Explosion)

MMS Investigation Report:

Completed

Activity:

Development/Production

Lease:

G02640

Event(s):

Fire / Explosion

Area:

Mississippi Canyon

Operation:

Production

Block:

148

Cause:

Equipment Failure / Human Error

Rig/Platform:

/ A

Water Depth:

65l feet

Remarks: While a contract employee was reconnecting turbine lines on the No. 1 generator, the No. 2 generator shut down. As a result, the platform shut in due to the loss of air supply to the ESD system. The emergency (diesel) generator was started after shut in, providing lighting to the Motor Control Center (MCC) building and other lights on the platform. There were three re-start attempts on the No. 2 generator, and each time it shut down due to no AC voltage. While going through a start up sequence of the No. 1 generator, everyone was in the MCC building when they heard a loud boom and rumble. The contractor operator stepped out the MCC building to investigate and he detected a small of burnt gas. While walking to the wellbay area, he heard a second boom. When he walked around the west side of wellbay, he encountered the heat of the fire and was driven back by it. He estimated that the fire covered approximately 80 percent of the wellbay. He alerted the platform personnel that there was a fire when he heard a third boom. He told the lead operator that the fire was out of control, and to get life jackets on and go to the survival capsule where he activated the abandon platform alarm. All personnel safely departed. The fire extinguished without any firefighting efforts.


16-Feb-2002 - Shell Oil Company

MMS Investigation Report:

None

Activity:

Development/Production

Lease:

G06896

Event(s):

Fire

Area:

Viosca Knoll

Operation:

Production

Block:

956

Cause:

Equipment Failure

Rig/Platform:

/ A (Ram-Powell)

Water Depth:

3,216 feet

Remarks: The operator was performing a turbine flush of the fuel gas compressor when an internal fire started in the turbine engine. There was a flash fire for one minute, and then the fire extinguished itself.


20-Feb-2002 - Shell Offshore Inc.

MMS Investigation Report:

None

Activity:

Development/Production

Lease:

G03936

Event(s):

Fire

Area:

Brazos

Operation:

Production

Block:

A 19

Cause:

Human Error

Rig/Platform:

/ B

Water Depth:

132 feet

Remarks: Extension cords being used by a construction crew came in contact with salt water causing a small flash fire. It was extinguished almost immediately by its own accord.


05-Mar-2002 - Spirit Energy Partners, L.P.

MMS Investigation Report:

None

Activity:

Development/Production

Lease:

00297

Event(s):