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Cheryl Anderson

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  Gulf of Mexico Region

Spills ≥ 50 Barrels (2,100 gallons)1983

January 20, 1983 - Texaco, Inc.

Pollution: 80 bbl Crude Oil Operation: Pipeline
Rig/Platform: Platform A Lease: G02937
Area: Block: West Delta
109
Cause: Weather Related & leak: storm & mud slide
Distance to Shore: 12 Miles Water Depth: 184 Feet
Pipeline Segment: 05767 Pipeline Diameter: 8 Inches
Other Events:

Remarks: A submerged oil pipeline was pulled apart by a mud slide approximately 500' from "A" platform. Bad weather with high winds and rough seas preceded the mud slide. Response: the two safety couplings were replaced along with 500' of pipe.


January 30, 1983 - The Superior Oil Company

Pollution: 800 bbl Oil based Mud Operation: Drilling & Barge
Rig: Platform: Rig Transworld 64
Platform 16
Lease: N/A
Area: Block: West Cameron
102
Cause: Equipment Failure & Human Error: transfer hose & negligence
Distance to Shore: 12 Miles Water Depth: 43 Feet
Other Events: Vessel Mishap

Remarks: 800 bbl of 85 ppg oil-based mud with 90 viscosity were pumped overboard while being offloaded to the barge. Apparently the hose parted but was not observed until after the mud had gone overboard. A barge with a vacuum cleaned up the residue.


February 1, 1983 -

Pollution: 125 bbl Crude Oil Operation: Production
Rig: Platform: Louisiana Offshore Oil Port (LOOP) Lease: LOOP
Area: Block: Grand Isle
59
Cause: Equipment Failure: transfer hose
Distance to Shore: 15 Miles Water Depth: 90 Feet

Remarks: A pollution incident occurred causing a 50-200 barrel oil spill when a transfer hose ruptured.


March 9, 1983 - CNG Producing Company

Pollution: 77 bbl Diesel from drilling mud Operation: Drilling & Motor Vessel
Rig: Platform: Rig Triton III (jack-up)
Well #4
Lease: G03792
Area: Block: South Pelto
15
Cause: Equipment Failure: transfer hose
Distance to Shore: 12 Miles Water Depth: 48 Feet
Other Events: Vessel Mishap

Remarks: EXPLORATION SPILL. While pumping 17.1 ppg oil base mud from the supply vessel to the rig, rig crew members at the mud pits saw there were no returns. They had the vessel crew stop the mud transfer pump. The 3" Evertite coupling was disconnected below the surface of the water. It is likely that the safety wire which prevents the connection from coming apart either failed or was not installed. Response: coupling was reconnected. Spilled 100 bbl of Invermul oil base mud (23% water, 77% diesel), or equivalent to a 77 bbl diesel spill.


March 20, 1983 - Exxon Corporation

Pollution: 320.4 bbl Diesel Operation: Drilling & Motor Vessel
Rig:
Platform:
Rig Penrod 89 (jack-up)
Well 3
Lease: G04733
Area: Block: High Island
170
Cause: Collision
Distance to Shore: 31 Miles Water Depth: 50 Feet
Other Events: Collision

Remarks: EXPLORATION SPILL. The workboat was tied up at the jack-up rig unloading cement and H2O. The workboat's anchor chain broke allowing the boat to drift over into the leg of the jack-up, knocking a hole in the fuel tank.


April 14, 1983 - Shell Offshore, Inc.

Pollution: 200 bbl Diesel Operation: Drilling & Motor Vessel
Rig/Platform: Platform B Lease: N/A
Area: Block: Eugene Island
189
Cause: Equipment Failure: transfer hose
Distance to Shore: 35 Miles Water Depth: 65 Feet
Other Events: Vessel Mishap

Remarks:

A diesel hose parted while offloading diesel from the workboat to a drilling rig allowing diesel to spill into Gulf waters. No pollution was detected in the waters the next morning, so 200 bbl may be an overestimate of the spill size.


May 9, 1983 - CNG Producing Company

Pollution: 77 bbl Diesel from Oil based Mud Operation: Drilling & Motor Vessel
Rig: Platform: Rig Triton III
Platform 4
Lease: G03792
Area: Block: South Pelto
15
Cause: Equipment Failure: transfer hose
Distance to Shore: 12 Miles Water Depth: 48 Feet
Other Events: Vessel Mishap

Remarks: While pumping oil-base mud from a supply vessel to the rig, the 3" Everlite coupling disconnected. This allowed 100 bbl of oil-base mud (77% oil) to be pumped overboard, so 77 bbl diesel spilled.


May 16, 1983 - Atlantic Richfield Company

Pollution: 95 bbl Diesel Operation: Drilling & Motor Vessel
Rig/Platform: Rig J-Storm XV Lease: G05185
Area: Block: West Cameron
250
Cause: Collision
Distance to Shore: 48 Miles Water Depth: 78 Feet
Pipeline Segment: Pipeline Diameter:
Other Events: Collision

Remarks: A workboat hit one of the rig's legs at midnight. There was a hole in the boat's fuel tank. The diesel spill dissipated during the night in heavy seas.


August 2, 1983 - Kerr-McGee Corporation

Pollution: 119 bbl Diesel Operation: Production & Motor Vessel
Rig/Platform: Platform K Lease: N/A
Area: Block: Ship Shoal
214
Cause: Collision
Distance to Shore: 37 Miles Water Depth: 105 Feet
Other Events: Collision

Remarks: Motor vessel accidentally bumped platform while unloading equipment, puncturing the fuel tank.


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Last Updated: 06/24/08, 02:42 PM

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