February
27, 2008 –
Kerr-McGee Oil & Gas
Corporation
| Pollution: |
682
bbl |
Crude Oil/ Condensate: |
None |
| Refined Petroleum: |
None |
Synthetic Oil Fluids*: |
None |
| Chemicals: |
682 bbl
Calcium Chloride (CaCl2) completion fluids |
Event: |
Pollution
|
| MMS Investigation Report: |
Accident Incident
Report Only |
Activity: |
Development/Production |
| Lease: |
G09191 |
Operation: |
Completion |
| Area: |
East
Breaks |
Causes: |
Human
Error |
| Block: |
688 |
Distance to Shore: |
135
Miles |
| Rig: |
Diamond Ocean
Valiant |
Water Depth: |
3,788
Feet |
Remarks: During
completion activities on the semisubmersible drilling rig Diamond Ocean
Valiant (built in 1989), calcium chloride completion fluid was being
pumped from the mud pits to the liquid storage leg. Approximately 682
barrels of calcium chloride (CaCl2) were released through the dump valve
and discharged into the water due to a valve that was inadvertently left
in open position.
NRC Reports: 863653
& 863655
March 19, 2008 –
Newfield Exploration Company
| Pollution: |
131.3 bbl
|
Crude Oil/ Condensate: |
None |
| Refined Petroleum: |
None |
Synthetic Oil Fluids*: |
131.3
bbl
Synthetic Base Fluids in 217 bbl of 60.5% SBM |
| Chemicals: |
None |
Event: |
Pollution |
| MMS Investigation Report: |
Accident Incident Report Only |
Activity: |
Exploration |
| Lease: |
G018292 |
Operation: |
Drilling |
| Area: |
Mississippi
Canyon |
Causes: |
Equipment
Failure |
| Block: |
800 |
Distance to Shore: |
50
miles |
| Rig: |
Diamond Ocean
Quest |
Water Depth: |
3,116
Feet |
Remarks: Seas of 18-22 feet
caused the riser boost line on the semisubmersible drilling rig Diamond
Ocean Quest (built in 1972 and refurbished in 1996) to break at
riser connection below rig. Concurrently, a compensator hose gave way
and repairs were being made to that before it was noticed that the boast
line had failed. 217 bbls of mud were lost before pump was shut off. The
check valve in the riser held and the rig was shut down due to weather,
extreme heave. Once weather permitted, drilling was able to resume
without repairing the broken riser boost line. The boost line repair was
delayed until conditions were safe to do so.
Approximately
217 bbl of 60.5% synthetic-based mud (SBM) were lost to
the Gulf of Mexico. It is estimated that the lost SBM contained
approximately 131.3 barrels of synthetic base fluids.
NRC Report: 865423
March 21, 2008 –
Shell Offshore Inc.
| Pollution: |
70
bbl |
Crude Oil/ Condensate: |
None |
| Refined Petroleum: |
None |
Synthetic Oil Fluids*: |
None |
| Chemicals: |
70 bbl
Monoethylene Glycol |
Event: |
Pollution,
Injury, & Evacuation |
| MMS Investigation Report: |
2010
Completed 9-May-2008 |
Activity: |
Development/Production |
| Lease: |
G15988 |
Operation: |
Production |
| Area: |
West
Delta |
Causes: |
Equipment
Failure |
| Block: |
143 |
Distance to Shore: |
18
Miles |
| Platform: |
A-Process |
Water Depth: |
369
Feet |
Remarks: On March 21,
2008, at 1105 hours, on Shell Offshore Inc.'s, Right of Way (ROW) OCS-G
15988, West Delta Block 143 A-Process
4-pile fixed
platform with skirts
installed in
Federal waters in 1990, an employee
was injured while investigating a glycol leak. The Injured Person (IP)
observed glycol leaking from a 1" line approximately 8' above the deck.
The IP used a step ladder to access the area and began removing
insulation to expose the leak. At that point, a 1" valve on the leaking
glycol line came free exposing the IP to the hot glycol. The IP jumped
off of the ladder, in an attempt to escape the hot glycol and suffered a
broken ankle and 1st and 2nd degree burns to his upper body. The
operator did not isolate or shut-in and bleed down the unit before
investigating the leak. The IP was not wearing the proper Personal
Protective Equipment (PPE) when exposing hot surfaces to avoid
burns.
As a result of the incident, 70 bbls of
monoethylene glycol (MEG) was spilled into the Gulf of Mexico. The
Glycol Regeneration Unit (GRU) was shut down and barricaded. The valve
was sent to Shell's Westhollow Research Center for analysis. Initial
findings suggest corrosion due to high pH from caustics introduced into
the system.
The primary causes of this incident were external
corrosion on MEG system and internal corrosion on galvanized nipple, and
failure to shut-in and bleed down equipment. A contributing cause may
have been due to the nipple that failed was galvanized steel not carbon.
High amounts of caustic probably contributed to the corrosion of the
nipple. Galvanized steel is more prone to corrosion.
Accident Investigation Report: Form
2010 21-March-2008 WD143
NRC Report: 865697
January to March,
2008 – Wild Well
Control (former BP Exploration & Production, Inc.)
| Pollution: |
53.7
bbl |
Crude Oil/ Condensate: |
53.7 bbl Crude
Oil |
| Refined Petroleum: |
None |
Synthetic Oil Fluids*: |
None |
| Chemicals: |
None |
Event: |
Pollution
|
| MMS Investigation Report: |
Completed 19-January-2008 |
Activity: |
Decommissioning/Salvage |
| Lease: |
01333 |
Operation: |
Submerged
Platform |
| Area: |
Grand
Isle |
Causes: |
Hurricane
Katrina |
| Block: |
47 |
Distance to Shore: |
18
Miles |
| Platform: |
C |
Water Depth: |
88
Feet |
Remarks:
The Grand Isle
47C 8-pile fixed platform installed in Federal waters in 1957, is one of
the seven BP operated platforms downed in Federal waters by Hurricane
Katrina in August 2005.
As part of BP's
initial hurricane response, over-flights were conducted as early as
September 6, 2005. In addition, an ROV vehicle was mobilized for
inspection of all of BP's downed platforms on October 20, 2005.
As of 2008, decommissioning and
abandonment operations are being performed by Wild Well
Control.
Approximately 50.6 bbl seeped from the
structure between January 1 and March 31, 2008. The Seahorse VI
was kept on location and deployed an absorbent boom for skimming
operations.
Accident Investigation Report: F2010
9-January-2008 GI47
2008 NRC Report: 859213
June 6, 2008 –
Murphy Exploration &
Production
| Pollution: |
180
bbl |
Crude Oil/ Condensate: |
None |
| Refined Petroleum: |
None |
Synthetic Oil Fluids*: |
None |
| Chemicals: |
180 bbl zinc
bromide |
Event: |
Pollution |
| MMS Investigation Report: |
Accident Incident Report Only |
Activity: |
Development/Production |
| Lease: |
G21790 |
Operation: |
Production |
| Area: |
Green
Canyon |
Causes: |
Human
Error |
| Block: |
338 |
Distance to Shore: |
103
Miles |
| Platform: |
A-Front Runner
Spar |
Water Depth: |
3,330
Feet |
Remarks: On the A-Front Runner Spar platform installed in Federal waters
in 2004, a dump valve was left open on storage
tank allowing 180 bbl of zinc bromide to spill into the Gulf of
Mexico.
NRC Report: 873341
Hurricane Gustav/Ike Narratives
Summary of Spills Linked to Major Hurricanes, 2002 to
2008
September
27, 2008 –
ATP Oil & Gas
Corporation
| Pollution: |
1,718.0 bbl
|
Crude Oil/ Condensate: |
None |
| Refined Petroleum: |
None |
Synthetic Oil Fluids*: |
1,718
bbl
Synthetic Base Fluids in 3,123 bbl of 55% SBM |
| Chemicals: |
None |
Event: |
Pollution |
| MMS Investigation Report: |
Completed 29-June-2009 |
Activity: |
Exploration |
| Lease: |
G16661 |
Operation: |
Drilling |
| Area: |
Mississippi
Canyon |
Causes: |
Equipment
Failure |
| Block: |
941 |
Distance to Shore: |
65
miles |
| Rig: |
Seadrill West
Sirius |
Water Depth: |
4.000
Feet |
Remarks: ATP Oil and Gas
reported a 3,123 bbl of 55% synthetic based mud (SBM) spill that
occurred late on Saturday, Sept 27, 2008.
It is estimated
that the lost SBM contained approximately 1,718.0 barrels of synthetic
base fluids. The new Seadrill West Sirius
semisubmersible drilling rig (built in 2008) was drilling Well #2 and
began taking on 4400 bbls of mud at approximately 2130 hours.
Shortly after the transfer began a shift change took place. When
the transfer was nearly complete it was noticed that the pit gains
weren't what they should be, and the level of pit # 3 was
decreasing. The mud in this pit was transferred to the
others. Investigation showed that two dump valves, one manual and
one pneumatic located 60 feet below the deck in a confined space were
leaking. The mud pit dump valve did not fully close, possibly
due to the accumulation of solids preventing it from seating. The
master dump valve's manual operator/position indicator was incorrect for
this valve and did not allow the full opening and closing of the
valve. There was no sheen associated with this loss of
SBM.
Accident Investigation Report: Form2010
27-September-2008 MC941
NRC Report: 885454
July to September, 2008 – Taylor
Energy Company
| Pollution: |
72.0
bbl |
Crude Oil/ Condensate: |
72.0 bbl
Crude Oil |
| Refined Petroleum: |
None |
Synthetic Oil Fluids*: |
None |
| Chemicals: |
None |
Event: |
Pollution
|
| MMS Investigation Report: |
Accident Incident Reports Only |
Activity: |
Decommissioning/Salvage |
| Lease: |
01333 |
Operation: |
Submerged Platform |
| Area: |
Mississippi
Canyon |
Causes: |
Hurricane Katrina |
| Block: |
20 |
Distance to Shore: |
19
Miles |
| Platform: |
A |
Water Depth: |
479
Feet |
Remarks:
The
Mississippi Canyon 20 A 8-pile fixed platform installed in Federal
waters in 1984, was
completely destroyed as a result of a mud flow incident during
Hurricane Ivan in September 2004. After Hurricane Ivan, the platform
was found to be lying on its side, submerged nearly 75% below the
mudline, approximately 800 feet from its original location.
Estimates for cleanup operations have ranged up to $500 million
(Taylor 2007).
As of June 2009, decommissioning and
abandonment operations at MC 20 A are the last activity for Taylor Energy which sold
and transferred all its other GOM properties to Ankor Energy in
2009.
Approximately 72.0 bbl seeped from the
structure between July 1 to September 30, 2008. Three pollution
domes were installed over three distinct plumes in May
2009.
NRC Report: 876336
December
3, 2008 –
Mariner Energy, Inc. &
Rowan Drilling
| Pollution: |
70.0 bbl
|
Crude Oil/ Condensate: |
None |
| Refined Petroleum: |
None |
Synthetic Oil Fluids*: |
None |
| Chemicals: |
70.0 bbl
Completion Fluids |
Event: |
Pollution |
| MMS Investigation Report: |
2010
Completed
27-January-2009 |
Activity: |
Development/Production |
| Lease: |
G02592 |
Operation: |
Completion |
| Area: |
South
Marsh |
Causes: |
Equipment
Failure |
| Block: |
149 |
Distance to Shore: |
74
miles |
| Rig: |
Rowan J.P.
Bussell |
Water Depth: |
234
Feet |
Remarks: While utilizing the
Rowan J.P. Bussell jack-up rig (built in 2005), approximately 33 barrels
(bbl) of Zinc Bromide (ZnBr2) and approximately 37 BBLs of a weighted
blend of Calcium Bromide (CaBr2) and Calcium Chloride (CaCl2) was
released into the Gulf of Mexico, resulting from an upset condition
during completion operations for Well D-1. The faulty
(leaking) new butterfly valve #2, located on the suction line manifold,
resulted in the undesired flow of completion fluid into the GOM through
the open pre-load tank #39. It is unclear from the investigation what
exactly caused the failure of valve #2. According to the Offshore
Installation Manager, the entire system is new, but this particular
valve may have been damaged due to weathering and inactivity since
installation.
Accident Investigation Report: Form2010
3-December-2008 SM149
NRC Report: 891651
One barrel (bbl) equals 42 U.S. gallons (gal)
| U.S. Coast Guard Spill Size Categories
|
MINOR |
MEDIUM |
MAJOR |
| Less than 238 barrels (Less than 10,000 gallons) |
238 to 2,380 barrels (10,000 to 99,999 gallons) |
2,381 barrels and more
(100,000 gallons and more) |
| Size Categories are for coastal and offshore waters and
are based solely on spill volume. |
Synthetic Oil Fluids*:
In deepwater
drilling, synthetic-based muds (SBM’s) are preferred over petroleum
oil-based muds (OBM’s) due to the SBM's superior performance properties.
The synthetic oils used in SBM’s are relatively non-toxic to the marine
environment and have the potential to biodegrade.
60%**: Indicates that for a
synthetic-based mud release, the exact percentage of volume of
synthetic base oil to total volume of mud released was not
available and 60% was used as a reasonable approximation.
75%***: Indicates that for an oil-based mud release, the exact
percentage of volume of base oil to total volume of mud released was not
available and 75% was used as a reasonable approximation. Diesel is
assumed to be the base oil in OBM unless otherwise
specified.